What our customers are saying

Battery Equaliser™ has been producing and distributing our unique patented battery additive since 1991. We regularly receive testimonial support from our satisfied customers internationally. Here is a selection of these testimonials.

If you want to send us a review, please use the following e-mail address: sales@batteryequaliser.com.au, use our form or call us if you have any questions: 0418 673 4200418 673 420


K-Tec Engineering

K TEC Testimonial rev .docxK TEC Testimonial rev .docxK TEC Testimonial rev .docx

P&O Services, Australia

“… Our satisfaction with the product has been sufficient for us to recommend that our entire fleet of in excess of 1000 floor scrubbing machines be dosed with Battery Equaliser as a cost effective means of preventative maintenance wherever lead acid batteries are used.”

PACS, Australia

“In reference to your Battery Equaliser product, we would just like to advise you of how impressed we are with the results we are getting from using your product. We have recently added your product in numerous battery operated equipment within our warehouse (forklifts etc) and have found that not only is the equipment running longer but also the charging time has been significantly reduced – hence we have less down time within our daily production and the required maintenance on each piece has also reduced…

Rio Tinto, Zimbabwe

“My initial test work with Battery Equaliser was carried out in an attempt to rejuvenate failed cap lamp accumulators. Thirty scrapped accumulators were treated and charged, of these sixteen were found to be serviceable, lasting up to ten hours. After six months ten accumulators are still in service…

Rustenburg Platinum Mines Ltd, South Africa

“I have noticed that here at Frank 1 shaft batteries have been a major maintenance headache. There were various reasons such as having five battery attendants to cover eighteen battery bays, poor tracking on battery tanks and general maintenance being of poor quality. I have sent attendants to Willard for training but we definitely will have to address the labour requirements. All this led us to our problems. I noticed good voltages but poor S.G’s. I came to hear about a product named Battery Equaliser…

Tauya Coach Services, Zimbabwe

“We have been using Battery Equaliser for the past three months. In spite of our initial scepticism towards the concept of improving upon poor quality batteries, we have had excellent results and have now decided to go ahead with using the additive in all batteries currently in use…

Traction Energy, South Africa

“Our company is a manufacturer of lead acid batteries in South Africa with 200 clients in our region. We have introduced the product, Battery Equaliser, as part of our ongoing service to our clients. Being aware of the various additives that have made similar claims in the past, we were initially dubious to the products’ effectiveness. We are however very pleased with the results achieved with this new product…

Trade Centre, South Africa

“We have been running tests with the Battery Equaliser product since November 1996. We were experiencing many problems with the batteries in our electric forklift vehicles and the cost of replacement was very high. We were at first sceptical of the product but having batteries which only ran for 2 or 3 hours was in itself a massive problem…

Engebretson Grupe Co Inc, USA

“I have worked here at Engebretson-Grupe co Inc for twelve plus years in many capacities. In those years I have seen and heard plenty of sales pitches. I, as a Product Operations Manager, am constantly looking how to improve our efficiency. We operate seven electric pallet jacks ranging for one-year-old 24-volt lifts to decade old 12-volt lifts. Dale and Glen Cassidy approached me the first week of May 1999, regarding a battery additive they were introduced into our area…

United States Marine Corps

“On August of 1998, GSM Company began a test of a product called Battery Equaliser. This is a liquid additive that when put into lead acid batteries will increase operating time and extend the life of the battery. The forklift used by the IMA supply section was used for the test. The fork lift was charged without the battery additive for two cycles. Its average operating time for the two charged cycles was 3.6 hours. After the two dry cycles the battery additive was added to the same battery. The fork lift went through two charging cycles. The average operating time after the Battery Equaliser was added was 6.4 hours of operation. This is an increase of almost three hours of operating time…

Pure Renewable Power

“Here is a picture of my really old electric forklift (Lansing Bagnall). The batteries were becoming less able to hold charge and didn’t provide a good discharge time. After I added Battery Equaliser the fully charged voltage went up and the usable amp hours increased…
Go to Shop